Xenon Detector Status - PowerPoint PPT Presentation

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Xenon Detector Status

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The shape of the newly delivered sealing (metal gasket) was wrong ! Does not fit the groove? ... RGA data with recycled gasket used as a reference ... – PowerPoint PPT presentation

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Title: Xenon Detector Status


1
Xenon Detector Status
  • Liquid Xenon Group

2
Outline
  • Detector Setup
  • Operation
  • Performance
  • Problems and solutions

3
Detector Setup
4
PMT installation completed
  • All PMT successfully installed in Aug 2007
    together with
  • LEDs
  • Alpha sources (plates and wires)
  • PT100 temperature sensors
  • Laser fibers
  • Surface level meter
  • lt 200300um gap btw inner slab and wall

xenon
g
5
Sensors, LEDs, and alpha sources
Capacitor-type surface level meter
Pt100 Temp sensor 22 sensors in LXe 21 sensors on
the wall
  • Two type of a sources
  • Plate 20 pieces
  • Wire 5x5 wires

LED 3 different attenuation x 10
6
Cabling and Al filler installation
7.5l
4.5l
  • Filler volume
  • Lateral 7.5lx6x2 4.5lx2x2 108l (design) 108
    7.5(US) 4.5(DS) 96l (reality)
  • Bottom 49l (design) 49 10 39l (reality)

7
We were ready to close but
  • The shape of the newly delivered sealing (metal
    gasket) was wrong !
  • Does not fit the groove?!
  • Radii were correct but they made a mistake in
    bending
  • Sent back to Garlok and repaired
  • While waiting repair work, old gaskets were
    recycled with indium foil around the corner
  • Vacuum test OK
  • But leak of the order of 10-4 mbarl/sec with 1
    bar xenon in the cold vessel

1 bar xenon
outgas
vacuum
Warm vessel vacuum
Xe leak
Mass spectrometer
8
RGA of leaking xenon
  • Doubly charged 132Xe (Xe) is used to evaluate
    amount of xenon in the warm vessel
  • Production cross section with 110keV electron is
    40 of Xe production
  • Used as reference data for later use

10-4 mbarl/sec leak
9
Closing the covers
  • Gaskets replaced with newly delivered ones on
    5/Sep
  • Super-insulator on the cold vessel
  • 240 Nmm torque

10
Pressure/leak test
  • Xenon gas (liquid) in the cold vessel
  • Mass spectrometer on the warm vessel
  • RGA data with recycled gasket used as a reference
  • Doubly charged 132Xe (Xe) is used to evaluate
    amount of xenon in the warm vessel
  • Production cross section with 110keV electron is
    40 of Xe production

10-4 mbarl/sec leak
11
Estimation of xenon leak rate
Recycled gasket 10-4 mbarl/sec leak Room
temperature xenon gas
New gasket Room temperature xenon gas
Better at low temperature
12
Operation
13
Gas/liquid system
Gas-phase purifier
Gas line
Liquid line
High pressure Storage
Detector
1000L dewar
Liquid-phase purifier
14
Evacuation and liquefaction
  • Evacuation started on 5/Sep
  • Thanks to cryo pump (AISIN)
  • 6.9x10-3 Pa in 3 days
  • Cooling started on 10/Sep
  • Liquefaction started on 15/Sep
  • Surface level was monitored with
  • Temperature sensors
  • Level meter (long and short)

Cryo pump
Xenon gas
0.11 MPa
0.133 MPa
15
Liquid transfer
  • Liquid transfer by pressure difference between
    two cryostats through a vacuum insulated pipe
  • Started on 17/Sep and completed on 20/Sep
  • 10 liter/hour transfer speed
  • Xenon filling was done in 15 days after starting
    evacuation

3m
16
End of xenon filling
temperature
Level meter
  • Additional 10 liter was transferred for assurance

17
How many liters of liquid xenon?
  • Cryostat volume 1200 liter
  • PMT and support 142 43 185 liter
  • Filler 135 liter
  • Lateral 96 liter
  • Bottom 39 liter
  • Cable 2030 liter
  • Additionally transferred amount of xenon 10
    liter
  • 1200 185 135 25 10 865 liter
  • Consistent with remaining amount of xenon in the
    dewar

18
Slow Control
Labview
megon00
PC in barrack
MEG Central DAQ System (SCFE)
For shift crew use
Labview
XEC PC 2
XEC dedicated SCFE Node cooperation Alarm to
experts
XEC PC 1
For expert use
Important controls are implemented in SCS nodes
Detector, storage, dewar, purifiers
19
Liquid circulation
Purifier Cartridge Molecular sieves, 13X 25g water
Freq. Inverter OMRON
  • Circulate xenon in liquid phase
  • Circulation pump
  • 100liter/h_at_3175rpm, Dp 0.2MPa
  • Molecular sieves
  • gt24 g water absorption

PT
20
Succeeded!
Circulation period
50.63Hz !
  • Circulation speed evaluation
  • change of the surface level after closing the
    inlet valve
  • 3.6 / 30sec 432 / h
  • 1 corresponds to 0.165 liter
  • 0.165x 432/h 71 liter /hour

21
Liquid-phase purification
  • Light yield for 17.6MeV g saturated around 23/Nov
    (180h purification time)
  • Necessary to continue longer than we expected
  • 5 hours purification was enough in the LP test
    (100L LXe)
  • Probably due to
  • slower circulation speed (100L/h ? 70L/h)
  • Worse initial condition compared to the LP
  • Needed longer time to prepare monitoring tools
    due to PMT HV feedthru problem (reported later)
  • Noise from the pump (freq. inverter?) affected
    other detectors

C-W run 17.6MeV gamma
22
Absorption Length
  • Ratio Data/MC vs distance fitted with an
    exponential curve.
  • Inner and Outer face PMTs
  • Cosine of incidence angle lt -0.2
  • Slope compatible with zero (no absorption).

l gt 3 m _at_95 C.L.
After 50 h purification, 4/Nov
Alpha source
PMT
23
Performance
2D display, charge/time
2D hist, chargePMT
3D reconstructed position
Waveform
1D histograms
Chargeevent
24
PMT Calibration
  • PMT calibration
  • LED
  • PMT gain
  • Flushing LEDs at different intensities
  • Npe1/s2
  • Time offset calibration
  • Viewing one LED flushing with many PMTs
    simultaneously
  • Alpha
  • QE and absorption length evaluation
  • Liquid and cold gas

25
Time offset determination
  • Possible method only in non-segmented detector
    like ours
  • c is obtained by using all data

Different LEDs viewed by one PMT
Measured
Flashing Time Of i-th LED
Speed of LED light
Offset of j-th PMT
Tj
RD run (ultra low)
ti ti-1
1/c
txe - tTC
li,j-li-1,j
26
C-W run
  • Li at 14.6, 17.6 MeV
  • B at 4.4, 11.7 and 16.1 MeV
  • Details in Giovannis presentation

27
CEX run - Pi0 calibration
  • CEX process
  • p-p?p0n
  • p0(28MeV/c) ? g g
  • 54.9 MeV lt E(g) lt 82.9 MeV
  • LH2 target
  • NaI tagging counter
  • 3x3 crystals, APD readout
  • Pb collimator panel in front of the Xe detector

g
28
LH2 Target
  • Pressure test of cell 4.5 bar (abs)
  • Time to liquefy
  • 80 min from start of LHe flow
  • Liquid stability
  • 1.2 bar operating pressure (96 cell full)
  • 1.3 RMS, 6 max excursion
  • Liquid Helium consumption
  • 2.4/h
  • 42h auto

29
NaI Detector
beam axis/- 21 (/- 0.07) deg.
Up/down/- 60 (/- 0.005) deg.
30
CEX run data analysis, preliminary
  • Position cut
  • Cut shallow events (lt 2cm)
  • Select only center events ( u,v lt 5cm)
  • Position correction
  • Pile-up rejection by light distribution
  • Select center event on NaI detector
  • Not applied QE correction
  • If applied worsen resolution.
  • Pedestal has 2 spread
  • Needs better baseline evaluation
  • Check hardware for 2008 run

55MeV gamma
pedestal
sup 2.4 FWHM 6.5
31
Time Measurement
Intrinsic resolution by T-B analsysis
  • Using only 12 PMTs around the center

115ps
  • T weighted mean of inner PMT timing after
    subtracting photon propagation time
  • Effective velocity 10cm/ns

32
Position Measurement
  • Using collimator run data,

33
Physics run
  • RD run gamma energy
  • Data Xe self trigger threshold3.5V
  • MC RD event generation event overlaps
    trigger simulation
  • Vertical scale is scaled assuming,
  • Mu stop 5e6
  • Calorimeter acceptance 0.1
  • Calorimeter detection efficiency 0.6

34
Problems found in 2007andsolutions for 2008 run
35
Feedthru
  • We could not apply required voltage on all PMTs
    at the beginning
  • We found that this had been caused by spark in
    the feedthru
  • Needed to prepare new ones for 2007 run
  • Commercial products or hand made?

36
How did we make new ones?
Watarus Design
Air
Metal body
Glass insulator
Xe
  • Production procedure
  • Fix pins in the holes and fill with silica
  • Bake in argon atmosphere
  • Cool down

No need to change connector Replacement can be
done quickly Body made of insulator (not metal)
37
Installation
  • Oct. 10-12 LXe recovery to 1000L Dewar
  • Oct. 13-14 GXe recovery
  • Oct. 15-16 Mounting new flanges testing
  • With flushing dry nitrogen gas in the cryostat
  • Oct 17-19 evacuation
  • Gas filling 0.13MPa
  • Successfully took gas alpha data at 800, 900,
    1000V
  • LED data
  • Liquid transfer started at almost same time
  • Until the detector is cooled we continued LED and
    alpha DAQ
  • 21, 22, 23/Oct transfer speed 1520 liter/hour
  • Completed early morning of 24/Oct
  • 2 weeks interruption of DAQ

38
PMT status after replacing feedthru
  • Stable operation after replacing feedthru
  • LED intensity optimization
  • Better gain evaluation than before

39
As a bonus
  • Xenon recovered through purifier
  • Practice to transfer the liquid to the dewar
  • Water contamination suppressed
  • Cryostat was warmed up to 220K
  • 1st experience of temperature cycle
  • Test of the gasket
  • RGA I 3.8x10-13A ? 5.7x10-7 mbarl/sec

132Xe
40
Future plan (currently ongoing)
  • Replacement during winter shutdown
  • 48 pin x 6 x 4
  • Need to change connectors
  • Used in the small prototype and PMT test chamber

ceramic
Kyocera Ultra High Vacuum Feedthrough
welding
41
Heat load
  • Pressure is slowly increasing under normal
    operating condition.
  • Refrigerator cooling power 200W
  • Expected redundant cooling power 100W
  • Calculation based on LP modeling
  • PMT37W (Vmean 775V)
  • Conduction64W
  • Cable (50), Chimney (4.8), SI(3.1), Support(6.3)
  • Heat income through Cu cooling pipes was not
    taken into account
  • Cu heat conduction 390 W/m/K
  • 10mm diam 1mmt pipe, 20cm
  • 390 x 135 (K) x 2.83x10-5/0.2 (m) 7.4W
  • 6 pipes ? 44.4W
  • Cf. Steel heat conduction 20W/m/K
  • There seems to be other heat leak
  • Larger than 50W
  • Super-insulator?

42
LN2 cooling pipe
  • Cu pipe feedthru ? SUS pipe feedthru

43
Cooling Power
44
Blow up of low temperature valve
  • Low temperature valves blew up
  • A few liters of liquid xenon was lost
  • Purifier cryostat was opened
  • Misleading valve design
  • No documentation on the manual
  • Piping was modified and no valve is in use now

Wilson Seal
Air
Wilson Seal
xenon
Plug or shaft
Cup nut
collar
bellows
O-ring
Liquid xenon
45
PMT Signal Splitter
  • Spark in feedthrus destroyed protection zener
    diodes on PMT splitter boards
  • base-line shift at splitter output
  • Signal was out of range of WFD
  • Fixed by replacing all zener diodes

DRS
splitter
PMT
Trigger
46
Light YieldDiscrepancy between a and g data
  • Energy scale discrepancy btw alpha and gamma
  • Too small light yield from g events (1/2)
  • Not due to magnetic field
  • Confirmed by taking C-W data w/o COBRA field
  • Purity seems good
  • Improvement and plateau of light yield of both
    gammas and alphas
  • Have a look on WF

a
47
Waveforms
  • ?triplet 22 ns
  • ?recomb 45 ns

ta 21 ns
tg 34 ns
! Careful treatment of electronics time constant
is necessary
Before purification
Q/A
was 1.93/-0.02 in LP test
A
Q
Electronegative impurity? Oxygen??
48
Electronegative Impurity Removal
  • O2 getter cartridge
  • Developed for LAr use at CERN
  • be mounted at the exit MEG liquid-phase purifier
    with by-pass valves
  • Preparing an oxygen purity monitor also
  • will be ready at an early stage of 2008 run

49
Current Status and Schedule
  • Xenon recovered to the 1000 liter dewar
  • Gas analysis will be done on site
  • Cryostat is opened now
  • All PMTs and cables are checked
  • Replacing feedthru is in progress
  • LN2 cooling pipe modification
  • Cryostat will be moved back to PiE5 at the end of
    March
  • Evacuation, liquid transfer, purification
  • Ready on 19/April
  • Schedule at http//meg.web.psi.ch/subprojects/inst
    all/xenon.html
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