Title: PT' PINDO DELI s Environment Performance Rating
1PT. PINDO DELI s Environment Performance Rating)
PT. PINDO DELI PULP AND PAPER MILLS
IS ONE OF PAPER INDUSTRY APP-SINAR MAS
GROUP LOCATED 60 km. EASTEN JAKARTA WEST JAVA
Karawang
2FACILITY TO PRODUCT 4 Paper Machines 1 Tissue
Machine 1 Corrugated Plant 1 Chemical Plant 1
Carbonless Paper Plant 7 Coating Plant 2
Converting Plant
- SUPPORTING FACILITY
- Power Plant 105 MVA
- PLN 45 MVA
- FWT Plant 27.000 M3/D
- WWT Plant 35.000 M3/D
- Land Fill 24.000 M3
- Pallet Work Shop 6.000 M3/M
-
3Paper Making Process
Water
Cleaner
Refiner
Cleaner Chest
Pulper
Pulper Tower
Mixing Chest
Stuff Box
Refiner Chest
Former Section
Head Box
Calender
Dryer
Pope Reel
Press Section
4PRODUCTION CAPACITY
PAPER (FC/ BOARD PAPER) TISSUE (PASEO) CORRUGATED
BOARD CHEMICAL NaOH CaCO3
865.000 TON/ ANNUM
58.000 TON/ ANNUM
38.000 TON/ ANNUM
110.000 TON/ ANNUM
240.000 TON/ ANNUM
5 MARKETS
SALES LOCAL
20 EXPORT 80
6WHY JOIN PROPER
- SAVE RESOURCES
- POLLUTION CONTROL
- NOT DEGRADE THE ENVIRONMENT
- IMPROVE COMPANY IMAGE
- EFFICIENCY
7OUR APPROACH
RELIGIOUS APPROACH Dont destroy what God/Allah
has excellently created
LEGAL APPROACH Obey all State Acts and
government regulations BUSINESS
APPROACH Improve efficiency
Lower cost
Increase profit
8WHAT HAVE BEEN DONE
-
- EMS (Evaluation and Reporting)
- CLEANER PRODUCTION/CPEE SINCE 1996
- - Good house keeping (Reuse, Recycle,
Recovery) - - Change of process
- - Change of technology
- final aim is to save resources control
pollution -
- CSR
- - Charity ? Giving fish
- - Community Development ? Giving rod to fish
9WHAT HAVE BEEN DONE
- EKOLABEL (Proper Mutual
- Requested)
- - Indonesia Ramah
- Lingkungan
- - Japan Ecolabel-Ecomark
- - Uero Ecolabe-Flower
Ecolabel Issue since 7 July 2006
10WHAT HAVE BEEN DONE
DEVELOPING PROPER 2003 2004 ? BLUE 2004
2005 ? BLUE 2006 2008 ? GREEN
Proper Grade Green
11CERTIFICATE OF APPRECIATION
CLEANER PRODUCTION 10 March 1996
ISO 9001 2000 Issue since 2 Jul.1996
12CERTIFICATE OF APPRECIATION
Appreciation by UNEP for the Implementation Greenh
ouse Gas Reduction
ISO 14001 2004 Issue since 14 Oct. 2004
13IMPACT of PROPER ON THE COMPANY
- smooth relationship better communication with
- surrounding community
- enhanced good image for all customers all over
- the world which promotes export
- more intent to obey all the environmental laws,
acts - and regulations
-
14CONDENSATE HEAT RECOVERY
- Investment/ system change
- 2 PM
- 1 TM
USD 200,000
- Annual cost saving
- 2 X 1,118.000 X USD 10/ ton steam
- USD 237,000/Year
- Annual steam saving 23.760 ton steam/yr
- Mean 23,760 X 77,3 1,836.648 NM3
EQ as 78975.864 tones gas
EQ 229,030 tones CO2 (Ref. Simplified GHG
calculator sheet)
15REFINER BLADE CHANGED
REFINER DIAGNOSTIC ( PLANNING ON END 2006 )
WHY ?
OVER 1 (ONE) GRADE OF CSR FREENES MEAN
ENERGY LOSS IS 72000 KWh FOR LINE PAPER CAPACITY
PRODUCT OF 100 TON/D . (Ref. DR. GATOT IBNU
SANTOSO PAPER ON 2004 DEPERINDAG)
ENERGY LOSS IS FOR PT. PINDO DELI PM 8/9S
REFINER - AVERAGE PRODUCT AS 2 X 850 MT/D
DIAGNOSTIC WAS DONE
POWER REDUCED
FROM 200 KWh/TP to 140 KWh/TP represented as CO2
39,8 CO2 / TP
16- Utilize paper process sludge as coal substitute
- (5 total caloric) for the CFB boiler
-
- Coal consumption (100) as 650 ton/day caloric
value 5500 KCal/Kg - Substitution at 5 X 650.000 X 5500
178.750.000 Kcal. - By sludge caloric value as 2000 Kcal.
As substitute - 178.750.000 / 2000 89.375 Ton
Coal/day Mean CO2 reduce as 27,108 Ton/annum
Also solved sludge landfill problem (ongoing
installation)
UNEP simplified calculator ,
www.uneptie.org/energy/tools/ghgin
17THANK YOU