Title: InVision%20Concept%20Modeler%20Program%20Review%20Engineering%20
1(No Transcript)
2InVision Concept ModelerProgram
ReviewEngineering Quality
3InVision Upgrades
- History
- v3.38
- v3.40
- Pause build on long cartridge change out
- Stop high vacuum condition
- Add baffle to Print head adaptor
- Addition of 2L vacuum bottle
- Change vacuum set point 5.00 5.75
inches of H2O - Replace nylon fittings with brass on Print head
adaptor - Grommet strips to clamp feed guides
- Modified needle housing collar (removed material)
- Removed potting from vacuum switch
4InVision Upgrades
- History
- v3.41 (Current)
- Add mechanical flags to stop support material
(S100) cartridge plunger 20mm short to stop
excessive air from entering the fluid delivery
system - Z guides added
- Grounding blocks to eliminate lead screws from
turning - New needle house stripper
- New needle housing coating heater
- Replace HMS bushings with bearing sleeves
5InVision Upgrades
- History
- v3.42 (Testing)
- Better positioning of cartridge to needle housing
- Tighter holding of cartridge
- Plunge to hold sequence modified to simulate drum
feed plunge movement while checking LOMS level - Reduce Pushed wax condition
- Reduce Mega pixel errors
- Reduce Ratio errors
- HMS damaged after Print head moves after
X-following error - Build material expiration change to 2 years
6Print head Adaptor
- v3.40 - Baffle
- Reduction of air entrainment Add baffle
(Support side only)
New print head part no. 300212-01
7Vacuum System
- v3.40 Stabilize vacuum system
- Add 2L bottle to stabilize operation of pressure
regulator / 0.5L remains
8Vacuum System
- v3.40 - Vacuum Stabilization
- Changed set point and switch of pressure
regulator to 5.75 H20 to better accommodate
material densities - Vacuum level being set at supplier location
- Vacuum setting confirmed at the contract
manufacturing location and adjusting in the field
should not be necessary - Resellers should not be adjusting vacuum levels
independent of 3D Systems knowledge
9Clamp Feed
- v3.40 - Guiding
- Grommet strips to cartridge guides
10Print head
- v3.40 - Print Head Priming
- Rotate Print head 135 to remove trapped air
- \\us-bur-na01\groups\US-GJ-MS03\Doc Control
Center\PUBLICATIONS\InVision\inverted printhead
procedure_Rev.zip - Provided inside upgrade kit
11Print head
12Plunger
- v3.40 - Software
- Single motion to a Plunge to Hold
13Plunger
- v3.40 - Software
- Single motion to a Plunge to Hold
Single movement of plunger to fixed position -
not based on LOMS level in adaptor Pressurizes
cartridge
14Plunger
- v3.42 - Software
- Implemented software 3.42 to improve cartridge
guiding during the plunge to hold move. This also
makes the plunge to hold move LOM sensor based
(currently in final test stages)
Step by step - Movement of plunger based on LOMS
level in adaptor
15Plunger
- v3.42 - Software
- Implemented software 3.42 to improve cartridge
guiding during the plunge to hold move. This also
makes the plunge to hold move LOM sensor based
(currently in final test stages)
Step by step - Movement of plunger based on LOMS
level in adaptor
16Needle Housing
- v3.41 New design
- Redesigned needle housing to improve ejection of
cartridge without hang
Old revision
New design
17Needle Housing
- V3.41 Design changes
- Redesigned needle housing to improve ejection of
cartridge without hang
Extended the bearing length of collar
Add Teflon hard coated both surfaces
18Clamp Feed
- V3.41 - Plungers
- Added stops to eliminate rotation of the plunger
screws
19Mechanical Improvements
- v3.41 - Z Guides
- Added Z guiding to cartridge guide path to
insure cartridges descend properly within clamp
mechanism
20Mechanical Improvements
- v3.41 - Software
- Implemented software 3.41 to eliminate air from
entering into the fuild delivery system
Any air in S100 support cartridge would enter the
fuild delivery system when cartridge 100
dispensed
21Mechanical Improvements
- v3.41 - Adding Flags
- Flags to stop the plunger 20 mm short to
eliminate excessive air from being pushed in
fluid delivery systems
Sensor
Added flags to stop the S100 support cartridge
200 mm to eliminate air in cartridge from
entering the fluid delivery system
22Print head Adaptor
- v3.42
- Larger Print head Adaptor with direct connect (no
tubes) - NEW
23Print head Adaptor
- v3.42
- Larger Print head Adaptor with direct connect (no
tubes) - OLD
24Print head Adaptor
- v3.42
- Redesigned Print Head Adaptor with larger
internal chambers
Surface Area Old design 1 300 mm2
New 2 077 mm2
25Print head Adaptor
- v3.42
- Redesigned Print Head Adaptor with larger
internal chambers
2.300 (58.4 mm)
1.400 (35.6 mm)
2.750 (69.9 mm)
Surface Area Old design 1 300 mm2
New 2 077 mm2
26Print head Adaptor
- v3.42
- Redesigned Print Head Adaptor with larger
internal chambers
2.300 (58.4 mm)
1.400 (35.6 mm)
Surface Area Old design 1 300 mm2
New 2 077 mm2
27Print head Adaptor
- v3.42
- Redesigned Print Head Adaptor with larger
internal chambers
Surface Area Old desgn 1 300 mm2
New 2 077 mm2
28Print head Adaptor
- V3.42
- Redesigned Print Head Adaptor with LOMS off-set
to accommodate difference in material densities
Support
Build
29Clamp Feed
- v3.42 - Alignment of cartridge tip to needle
housing - Moved clamps inward to center cartridge to the
needle housing
30Clamp Feed
- v3.42 - Alignment of cartridge tip to needle
housing - Moved clamps inward to center cartridge to the
needle housing
Cartridge
Clamp
Needle housing
Cartridge Tip Needle Housing aligned properly
Cartridge Tip
Cartridge not held snug Cartridge tip not aligned
to needle housing
31Clamp Feed
- v3.42 - Alignment of cartridge tip to needle
housing - Moved clamps inward to center cartridge to the
needle housing
Cartridge
Cartridge tip not aligned to needle housing
Needle
32Clamp Feed
- v3.42 - Alignment of cartridge tip to needle
housing - Moved clamps inward to center cartridge to the
needle housing
Cartridge
Cartridge tip is better aligned to needle housing
Needle
33Invision Clamp Feed System
34HMS / Software
- v3.42 Program change
- Redesign the build carriage to use bearings and
eliminate use of bushings - X Following error caused by excessive force
- Print head homes while the HMS engaged
Bearing part number 11855-119-00 Need to order
2 bearings
35Material Improvements
- SR200/HR200/DP200
- 2 year expiration date build material
manufactured after 01-Jan-2007 - Eliminate unnecessary RMA / Returned material
- Customer complaints on receipt of material with lt
6 months expiry date - Software v3.42 will accommodate material produced
prior to 01-Jan-2007 - Added stabilizer to eliminate clogged jets, waste
tanks and waste umbilical when build and support
materials reacting when co-mixing
36RMA / Returns
- All part returns should be coordinated with Frank
Vullhorst - Non-conforming parts should be returned to UPS
Col. Using a RMA