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The Three Mile Island Disaster

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TMI 1 and 2, each with its own reactor and power generating equipment. ... This would lead to the fuel rods overheating, which could in turn lead to a meltdown. ... – PowerPoint PPT presentation

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Title: The Three Mile Island Disaster


1
The Three Mile Island Disaster
  • The Three Mile Island Nuclear Power Plant was
    split into 2 Units. TMI 1 and 2, each with its
    own reactor and power generating equipment.
  • The incident occurred on March 27, 1979 in TMI-2.
  • The reactor was operating normally and at 97 of
    its 1000 Megawatt capacity.

2
The TMI-2 Reactor
  • Like any nuclear power plant, the TMI system was
    split into 3. This is to keep the radioactive
    reactor coolant contained.
  • The Primary Loop, which includes the reactor and
    the coolant.
  • The Secondary Loop, which deals with the actual
    power generation.
  • And the Tertiary Loop, which cool the plant and
    contains the large cooling towers.
  • For this incident we are only concerned with the
    Primary and Secondary loops.
  • Each loop relies on the other working correctly.

3
The Primary Loop
  • The Reactor core heats up the surrounding coolant
    water.
  • This water then passes through the steam
    generator, which is essentially a heat exchanger.
  • The cool water then carries on through the
    primary loop and back to the reactor core.
  • The pressuriser maintains the correct water
    pressure in the loop by creating a controlled
    steam bubble.

4
The Secondary Loop
  • The steam comes from the steam generator and
    passes through the safety valves into the
    turbine, which produces the electricity.
  • The steam then passes into the condenser.
  • The now cool feedwater returns to the steam
    generator.

5
Feedwater Shutdown
  • A high pressure water line connected in error to
    the feedwater valve control air line.
  • Water forces its way into the valve control
    system.
  • Water reaches the valve controls
  • Almost every valve in the feedwater system slams
    shut, starving the Once Through Steam Generators
    (OTSGs) of feedwater.

6
Emergency Feedwater Pumps Started
  • These pump fresh feedwater into the OTSGs to
    take the residual heat out of the reactor.
  • However, the feedwater had been blocked from
    these pumps during routine maintenance and never
    restored.
  • The indicator showing this was covered by a tag,
    and operators didnt check it.

7
Turbine Trip
  • The plants safety systems trip the turbine, to
    try and stop the steam generators from boiling
    dry.
  • This diverts the steam straight into the
    condenser.
  • Due to a design flaw, the condenser tripped,
    which meant that steam was vented into the
    atmosphere and feedwater is lost.

8
Reactor Trip
  • Due to the loss of feedwater, the OTSGs were not
    taking heat from the primary loop coolant.
  • This caused the pressure and temperature in the
    reactor vessel to rise.
  • The control system detected this and tripped the
    reactor.

9
Automatic Pressure Relief Valve Opens
  • As the heat in the Primary system increased, so
    too did the pressure, so the automatic relief
    valve was opened.
  • This vented steam into a quench tank.
  • However, the valve was faulty, and did not close
    as it should of done.
  • The indicator on the control board showed
    otherwise, as it showed what the valve had been
    instructed to do, rather its actual status.

10
Extra Coolant Pumps Started
  • As the reactor coolant cooled and shrank the
    water level in the primary loop dropped.
  • To make up for this extra coolant was pumped into
    the reactor vessel.
  • The water level steadied then began to rise
    quickly.
  • A very dangerous situation was developing the
    primary loop should never be full of water.

11
Steam Generator Boils Dry
  • As the emergency feedwater valves were still
    closed no water was getting into the OTSGs.
  • This meant that no heat was being taken out of
    the steam generators. This in turn led to a
    temperature rise in the primary loop.
  • The staff didnt realise why, as they didnt know
    that the valves were closed.

12
Primary Loop Temperature Rises
  • Because there was no feedwater going to the
    OTSGs the temperature was not being taken from
    the reactor coolant.
  • Due to the open relief valve pressure, however,
    was dropping.
  • This confused the operators as generally if
    temperature rises, so does the pressure.

13
Disaster Approaches
  • If the primary loop pressure fell low enough or
    the temperature rose enough then the coolant
    would boil.
  • This could lead to the fuel rods being uncovered
    and cooled only by steam.
  • This would lead to the fuel rods overheating,
    which could in turn lead to a meltdown.

14
Further Relief Valves Opened
  • Too much coolant could be disastrous, as if the
    primary loop was full then any shock could be
    enough to damage coolant pipes or pumps, leaking
    yet more coolant.
  • To try and stop this the operators opened release
    valves to try and combat the rising coolant water
    level.
  • As the pressure dropped even more, automatic
    systems started pumping coolant back into the
    reactor vessel.
  • The operators, not knowing the relief valve was
    open shut them down.

15
The Twelve's are Closed!
  • Finally, one of the operators stopped eating his
    doughnuts and decided to check the feedwater
    system.
  • He moved the paper tag and noticed that the
    emergency feedwater valves (12A and 12B) were
    closed.
  • He opened them and feedwater at last entered the
    OTSGs and began to take some heat from the
    reactor.
  • The temperature rise slowed, but didnt stop.

16
Main Coolant Pumps Shut Down
  • As the relief valve was still venting pressure,
    and the temperature was high the coolant began to
    boil.
  • Steam bubbles moved through the system until they
    got to the main coolant pumps.
  • These began to vibrate as they strained to move
    the steam.
  • The operators had to shut them down before they
    got damaged and caused a coolant leak.

17
Reactor Core Uncovered
  • As there was now no movement in the coolant,
    steam bubbles began to form.
  • One such bubble formed in the top of the reactor
    vessel.
  • This pushed the water level below the top of the
    core, which began to overheat as it became
    uncovered.

18
Human Errors
  • One of the operators suspected that the relief
    valve may be stuck, so he asked a technician for
    a temperature reading. A high reading would
    indicate that it was open.
  • The technician read the wrong reading, instead
    giving the temperature of another, normal valve.

19
Human Errors
  • The steam that was venting from the relief valve
    was routed to a quench tank. This tank
    eventually filled and broke a safety disk.
  • This caused the radioactive water to flood the
    containment building.
  • One of the operators decided to check the level
    in the quench tank, but only after the safety
    disk had broken and the level was normal.

20
Fresh Eyes
  • As the new shift began to arrive one of the
    engineers spotted the link between low pressure
    and high temperature.
  • He closed another valve, between the stuck relief
    valve and the quench tank.
  • As he did this the coolant pressure began to
    rise.
  • This was around 2 hours into the emergency.

21
Evacuation
  • The water that had leaked into the containment
    building found its way into the plants auxiliary
    building, via the drains.
  • This caused the radiation alarms to sound, and
    the building was evacuated.
  • A site emergency was then declared, and nearby
    towns began to be evacuated.

22
Core Status
  • At this point the operators had no idea of the
    status of the core, or the water level inside the
    reactor vessel.
  • No water level sensors were installed as they
    were not deemed necessary.
  • The temperature was not known either, as the
    software was only calibrated up to 700 degrees.
  • A team was sent directly to the cables from the
    reactor core to read the thermocouple directly.
  • They found the temperature was around 10,000
    degrees!

23
Hydrogen
  • When the material that was used in the fuel rod
    cladding is exposed to steam and high
    temperature, a chemical reaction occurs.
  • The cladding is destroyed and hydrogen released.
  • This hydrogen collected in both the reactor
    vessel and the containment building atmosphere.

24
Explosion
  • The hydrogen in the containment building was
    ignited by a spark from a relay.
  • The resulting explosion was as powerful as
    several thousand pounds of explosive, and created
    around 80psi of strain on the containment
    building.
  • Luckily, this was easily absorbed by the over
    engineered structure and no damage was caused.

25
Hydrogen In The Core
  • The hydrogen in the core was bad news, as
    hydrogen is even worse a coolant than steam.
  • Also, while the steam bubble could be relatively
    easily dispersed, hydrogen is much harder to
    remove.
  • There was a risk that because of the radiation,
    water could break down and release oxygen into
    the core.
  • Calculations indicated that 5 oxygen would be
    enough for an explosion and with 11 oxygen the
    oxygen/hydrogen mixture would self-ignite.

26
Getting The Reactor Cooled
  • At first pressure was dumped to allow a
    low-pressure pump to get some coolant into the
    primary loop. But the main coolant pumps needed
    to be restarted.
  • The automatic safety systems would not allow it
    to start because of the abnormal reactor
    conditions.
  • Eventually, these systems were overridden and the
    pump started.
  • 15 hours after the onset of the incident, the
    reactor was being cooled again.

27
Removing The Steam Bubble
  • Over the next few days the steam and hydrogen
    bubble had to be removed from the reactor vessel.
  • Although some of this was done chemically, they
    had to vent some radioactive gas into the
    atmosphere. There was still a fear of a hydrogen
    explosion.
  • It is believed that the reactor vessel contained
    at least the 5 oxygen required for combustion
    for at least 24 hours.

28
The Aftermath
  • Every one of the 36,000 fuel rods in the core had
    ruptured, contaminating the primary coolant with
    radioactive gases.
  • For 2 hours, over 70 of the core had been out of
    water.
  • The core itself was little more than rubble.
  • Parts of the core had reached over 4000 degrees,
    only a few hundred below the fuel rods melting
    point.

29
The Aftermath
  • Thousands of curies of radioactive gases had been
    released into the atmosphere.
  • Radioactive water had been dumped into the
    Susquehanna river.
  • The last venting of gas occurred in 1981.
  • All of the contaminated water has now been
    evaporated.
  • Most of the fuel has been removed and radiation
    levels are relatively low.
  • The unit will be completely decommissioned in
    2005, at the same time as TMI Unit 1.

30
RTS Issues
  • Why were the water and air lines compatible?
  • Why was the plant allowed to function when the
    emergency feedwater was blocked?
  • Why were the indicators on the control panel
    covered?

31
RTS Issues
  • The plant warning system was clearly inefficient
    the warnings were being printed, but the
    printer was 2 hours behind due to the number of
    warnings.
  • Message Prioritisation?
  • There was no warning at all of the stuck release
    valve? The system only showed what the valve had
    been commanded to do, rather than its actual
    status.

32
RTS Issues
  • Why was there no indicator of the status of the
    quench tank safety system?
  • One of the technicians gave a reading from the
    wrong valve user incompetence or bad design?
  • The system had to be over-ridden before the
    coolant pumps could be restarted. Again, bad
    systems design?
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